The generator and lead were received for analysis on 06/02/2016.Product analysis for the lead was completed and approved on 06/23/2016.Note that a portion of the lead assembly including the electrodes was not returned for analysis; therefore a complete evaluation could not be performed on the entire lead product.During the visual analysis the bilumen tubing appeared to be twisted, in several areas and the end appeared to be twisted / abraded open / torn.During the visual analysis the connector pin tri-filar coil appeared to be broken in two areas.Scanning electron microscopy was performed on the connector pin tri-filar coil break as having evidence of a stress induced fracture (rotational forces) which most likely completed the fracture with mechanical damage.The area on another broken coil strand was identified as having evidence of a stress induced fracture (fatigue appearance) with mechanical damage, pitting and evidence of a stress induced fracture (rotational forces) which most likely completed the fracture.The area on the last broken coil strand was identified as having what appeared to be evidence of a stress induced fracture (fatigue appearance) with mechanical damage, no pitting and residual material.Scanning electron microscopy was performed on the connector ring tri-filar coil break and identified the area on one of the broken coil strands as being mechanically damaged (smooth surfaces) with pitting which prevented identification of the coil fracture type.The area on the remaining broken coil strands was identified as having evidence of a stress induced fracture (rotational forces) which most likely completed the fracture with mechanical damage on both and pitting on one of the broken coil strands.Pitting was observed on the coil surface.It is believed that stimulation was present for a certain period of time as evidenced by the presence of metal pitting.The abraded openings / torn area found on the bilumen tubing, most likely provided the leakage path for the dried remnants of what appeared to have once been body fluids inside the bilumen tubing.With the exception of the observed discontinuities and abraded opening the condition of the returned lead portion is consistent with conditions that typically exist following an explant procedure.No other obvious anomalies were noted.The setscrew marks found on the lead connector pin provide evidence that, at one point in time, a good mechanical and electrical connection was present.Continuity checks of the returned lead portions were performed, during the visual analysis, with no discontinuities identified.Product analysis for the generator was completed and approved on 06/27/2016.The returned decoder shows that the ¿diagvinitialprechange¿ value is 4523 ohms while the ¿diagvinitialpostchange¿ value is 13568 ohms, and the time of change detection (b)(6) 2016 (explant (b)(6) 2016).Various electrical loads were attached to the pulse generator and results of diagnostic tests demonstrate that accurate resistance measurements were obtained in all instances.In addition, the septum was not cored, thus eliminating the possibility of a potential unintended electrical current path through body fluids.In the pa lab, the device output signal was monitored for more than 24-hrs, while the generator was placed in a simulated body temperature environment.Results showed no signs of variation in the pulse generator¿s output signal and demonstrated that the device provided the expected level of output current for the entire monitoring period.The pulse generator diagnostics were as expected for the programmed parameters.In addition, a comprehensive automated electrical evaluation showed that the pulse generator performed according to functional specifications.There were no performance or any other type of adverse conditions found with the pulse generator.
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