Edwards received notification from a field clinical specialist that during a transfemoral tavr, when the 29mm s3 valve was being inflated, the commander balloon ruptured.The valve was in a stable position.It was attempted to pull the balloon back into esheath, however, this was unsuccessful.The team cut the commander system and removed the system from the patient.When pulling the device out, the nose cone and half of the balloon got dislodged, leaving the nose cone and a piece of balloon inside the patient.An attempt to snare the devices was performed unsuccessfully.Finally, it was decided to place a covered stent over the separated components.The right liac and femoral vessels 'looked good' post deployment of the covered stent.Patient was in recovery in stable condition.
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The device was not returned for evaluation.Therefore, a no product return engineering evaluation was performed.The device history record (dhr) review did not reveal any manufacturing nonconformance issues that would have contributed to the event.A review of edwards lifesciences risk management documentation was performed for this case.The reported event is an anticipated risk of the transcatheter heart valve procedure, additional assessment of the failure mode is not required at this time.The complaints of balloon burst, distal tip separation, and withdraw difficulty were unable to be confirmed since neither the applicable imagery nor the complaint device were returned for evaluation.Due to the unavailability of the complaint device, engineering was unable to perform any visual inspection, functional testing, or dimensional analysis.Therefore, the presence of a manufacturing non-conformance was unable to be determined.An existing edwards' technical summary has been documented for root cause analysis on balloon bursts in a calcified landing zone.The technical summary provides a rationale as to why it is unlikely that a product defect or manufacturing non-conformance contributed to this type of event, including factors on why deployment of balloons on thv delivery systems are subject to increased risk of burst in a calcified landing zone.As per 3mesio provided, there was calcium present in the patient.The presence of calcification can create a challenging anatomy for balloon inflation.While the balloons are sufficiently designed and tested for rated burst pressures well above their inflation pressure, calcified nodules can compromise the structure of the balloon wall via following mechanisms such as puncture, local overstretching, open cell impingement, or stress concentration.As the balloon was burst, the altered balloon profile can be more susceptible to catch on the distal end of sheath tip which would have then led to the experienced retrieval difficulty.As a result, additional pull force/excessive device manipulation could have been applied to overcome the withdrawal difficulty which then led to the reported separation.In addition, the technical summary outlines the extensive manufacturing mitigations in place to prevent this type of malfunction (visual and dimensional inspections, leak testing, and functional balloon burst testing that occurs with every manufactured lot).These inspections and testing further support that it is unlikely that a defect present in manufacturing contributed to the complaint.The technical summary also outlines the instructions for valve deployment.It should be noted that these mitigations are still in place.Review of available information suggests that patient factors (calcification) contributed to the balloon burst while procedural factors (withdrawal of burst balloon, excessive manipulation) contributed to the withdrawal difficulty and separation.Since no edwards defect was identified, no corrective or preventative action is required.Complaint histories for all reported events are reviewed against trending control limits monthly, and any excursions above the control limits are assessed and documented as part of this monthly review.
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