It was reported that a pipe burst and squirted water onto the analyzer.The customer requested that an engineer check it before turning it back on.The field service representative removed the covers and inspected the analyzer.He observed some watermarks on the printed circuit board (pcb) but found it still functioning correctly.He observed that water was still in the tray and reagent compartment but had dried.He performed tests that showed the analyzer was working within specification.It was reported that the customer observed issues with fluctuating signals and qc.A new reagent lot was calibrated and it was noted there was some foam on the reagents.The qc was out of range.After the bead mixer was adjusted, no foam was observed on the reagents.It was noted the pretempering was performed for 30-60 minutes and rack adapters were not in use for all racks.It is recommended to increase the pretempering time for reagent handling.The customer freezes primary tubes, which is not recommended and increases a risk for issues with sample quality/sample pipetting and results.It was noted that the air conditioner was very close to the analyzer.Installing the instrument close to the air conditioner should be avoided due to possible emi (electromagnetic interference) or on the way of the air conditioner air flows due to possible changes in the air humidity that may affect liquid level detection system.The customer refused to relocate the analyzer.Another service visit occurred.A field service representative performed precision studies under controlled conditions (the air conditioner was switched off and the reagent was pretempered 1 hour).Any outstanding maintenance was performed by the field service representative (daily maintenance, pinch valve tubing replacement, and liquid flow cleaning).The calibration signals were within expected ranges and the precision test was acceptable.The reagent kit was checked after the runs as the remaining determination was 10: bubbles were observed on the surface of the bead compartment of the reagent pack.The remaining determinations/shots in the reagent pack were used to assess roche qc performance at the end of the reagent pack, which were within specification.A sample liquid level detection malfunction was observed during movement and sample volume insufficient or clot pip.Alarms were found in the alarm trace, which may be linked to a sample handling issue.The instrument check was within specifications.Based on the available data, information, and service visits, there are major hints for local issues as root cause (sample handling/ improper preanalytics, reagent handling, general problems with the instrument and work processes).Although the most recent instrument checks were within the specs, instrument-related issues cannot be excluded.Additionally, wetting of the pcb occurred.Due to this fact, it is not possible to guarantee instrument performance.A generic reagent issue is not evident.
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