Product event summary: initial analysis confirmed the reported event of "810" errors, main printed circuit board (pcb) was out of electrical specification.It was also noted that the keypad looked to be lifted a little above the doo button and contaminated below the button on the inside, the ring attachment looked contaminated, the display glass surface was contaminated, the encoder flex, all encoders were twisted, however, they were working when tested and within part specifications.Functional testing failed due to main pcb.The device powered up after device log reset from incoming functional testing.Failure analysis was performed on the device.The log showed multiple occurrences of the 810 error, this error indicates the occurrence of a device self-test failure.There were also occurrences of a 721 error, this error indicates a capacitor voltage above high threshold.Visual inspection revealed residue on the inside surface of the viewing window of the keypad, the residue appeared to be the result of liquid ingress around the doo button through separated layers of the switch membrane keypad.No visual anomalies observed on pcb.Bench analysis revealed no errors after the initial 810 error was cleared.Could not reproduce failure modes resulting in logging of either the 810 or 721 error codes.The keypad was sent to the chemical technologies lab for analysis.Residue was determined to be primarily consistent with that of a surfactant/detergent - sodium dodecylbenzenesulfonate.No anomalies were found with solder joint integrity.Conclusion: the 0810 and 721 error code producing failures could not be reproduced.Inspection revealed residue on the inside surface of the keypad viewing window indicative of fluid ingression.It was determined this was caused by keypad layer separation in vicinity of the doo button.
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