Submission of this report does not constitute an admission that the manufacturer's product caused or contributed to the event.A field service engineering (fse) was at customer's site to resolve reported event.Fse confirmed reported errors by reviewing the qc data.Fse noted that the analyzer was due for periodic maintenance (pm) and performed the analyzer pm.During verification of substrate replacement, fse noticed an inconsistent purge of substrate, as well as a slow drip after dispensing.Fse inspected the 3-way substrate solenoid valve and observed debris in the first port of the valve, which receives from the substrate bottle.Fse replaced the 3-way solenoid valve, and successfully validated analyzer by running calibration, precision and qc; all runs completed without errors and within acceptable range.No further action required by field service.The aia-360 analyzer is functioning as expected.A 13-month complaint history review and service history review through aware date of event for similar complaints was performed for serial number (b)(4).There were no other similar complaints found during the searched period.The aia-360 operator's manual under chapters 9 - 10, provides detailed information on substrate line maintenance procedure.The 3-way solenoid valve was returned to tosoh instrument service center for investigation.Functional testing did not confirm the reported failure.The most probable cause of the reported event could not be reproduced.
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A customer reported getting out of range high results on quality control (qc) imprecision during sample runs with the aia-360 analyzer.The customer stated qc was rerun with fresh qc material, but that didn't improve the results.The customer also reported hearing noise from carousel turntable.The customer stated some of the reagent test cups on the carousel had fluid on the outside of the cup and fluid on the carousel.Technical support specialist (tss) instructed the customer to verify proper functioning of the waste pump; the customer confirmed waste was going into the waste container and no waste tubing was pinched.Tss then, instructed the customer to inspect the bf probe and run a bf wash prime; the customer confirmed no leaks or fluid found, and tubing were attached.A field service engineer was dispatched to address the reported event, which resulted in delayed reporting of patient samples for cardiac troponin i (ctnl 2).There is no indication of any patient intervention or adverse health consequences due to the delay in reporting of patient results.
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