As reported by an edwards lifesciences affiliate in (b)(4), during implant of a 29 mm sapien 3 valve in the mitral position via transseptal approach the valve was unable to fully deploy due to delivery system leakage.The delivery system and valve were removed without issue.No valve was implanted.The patient was doing well post procedure, however later expired.Additional information requested was not forthcoming.
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The product was not returned for evaluation.Imagery provided by the site shows the valve on the inflation balloon partially out of the non edwards sheath.The inflation balloon is bunched up with the valve struts partially expanded and bent outwards.Leakage can be noted on the crimp balloon as liquid can be seen leaking from the region distal to the end of the balloon shaft.A device history records (dhr) review did not reveal any manufacturing related issues that would have contributed to the complaint.A review of the lot history revealed no other similar complaints.The instructions for use (ifu), device preparation and the training manual were reviewed for instructions or guidance for proper use of the device and no deficiencies were identified.During the manufacturing process, the delivery system is visually inspected and tested several times.During manufacturing, the delivery system balloon was 100% inspected.During the final inspection the delivery system underwent 100% inspection by both manufacturing and quality.Additionally all manufacturing lots are subject to product verification (pv) testing on a sampling basis.All samples passed product verification testing for this lot number.These inspections and tests during the manufacturing process support that it is unlikely that a non-conformance contributed to the reported complaint. a review of edwards lifesciences risk management documentation was performed for this case. the reported event is an anticipated risk of the transcatheter heart valve procedure, additional assessment of the failure mode is not required at this time. the complaint for balloon torn was confirmed based on the provided imagery.Investigation of complaint history, dhr and lot history review revealed no indication that a manufacturing non-conformance contributed to the event.A review of manufacturing mitigations supports that the delivery system has proper inspections in place to detect issues related to the complaint events.A review of ifu/training materials revealed no deficiencies.As mentioned in the description ¿when the physicians tried to pass the valve through the atrial septum, there was resistance and they inflated a bit the bottom of ew commander balloon (the valve was crimped on it) with the objective of increasing the size of the puncture site in the septum.¿ it is possible that by inflating the balloon in this manner the balloon material became damaged either by coming into contact with patient anatomy or from pressure build-up when inflating in the septum.As such when attempting to withdrawal the partially inflated thv back into the septum and out of the patient, additional force was likely applied as evidenced by the bunching of the inflation balloon leading to the balloon damage propagating and tearing radially.While a definitive root cause is unable to be determined, available information suggests that procedural factors (improper use of thv for dilating septum/withdrawal of partially deployed valve/excessive manipulation) may have contributed to the complaint events.The complaint was confirmed, but no manufacturing nonconformance was identified during the evaluation.No labeling/ifu/training inadequacies were identified.As such, neither a product risk assessment escalation, nor corrective or preventative actions are required.
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